DGCA inquiry rules out conspiracy in air scare for Rahul's plane

ANI  |  New Delhi [India] 

The of Civil (DGCA) in its investigation report related to air scare on Rahul Gandhi's flight in April has ruled out any conspiracy and blamed human error for a situation that led the plane to descend to dangerous levels after auto disengagement for 24 seconds.

The report said that a yaw damper failure occurred due to intermittent behaviour of FCC 2, this caused the auto pilot to disengage and the aircraft went into excessive right with altitude loss. Due to lack of situational awareness, the crew's actions to control of the aircraft manually were slightly delayed.

An inquiry was ordered after reports claimed that Gandhi's flight had "nosedived" en route to Hubli in in April this year and the had alleged a foul play in the incident.

However, the inquiry ruled out any conspiracy. "It was observed that the aircraft (VT-AVH) was cruising at FL 410 (41,000 feet) when auto pilot tripped. As the auto pilot tripped, both the crew observed YD (white) on Pilot Function Display (PFD). However the crew did not realize that the aircraft has gone into a with yaw damper failure. The crew only realized when the angle warning came at 45 degree i.e after 13 seconds of autopilot disengagement," the report said.

"The kept on increasing with altitude loss and reached a maximum of 64.95 degrees i.e 15 seconds after the auto pilot disengagement and altitude loss of 735 ft from the assigned flight level. The crew initiated corrective action to control the aircraft altitude 15 seconds after the auto pilot disengagement. The aircraft was finally recovered to straight and level flight after 24 seconds from the autopilot disengagement. From the above it is inferred that the crew actions were slightly delayed to take the corrective actions," the report added.

Gandhi was in Aircraft VT-AVH during his campaign trail in assembly elections. "The PIC actions were slightly delayed as he took over control manually only after the warning was activated. This delayed actions caused the aircraft to reach value and altitude loss which created panic and scare for the passengers in the cabin," the report said.

The has recommended corrective training for the cockpit crew and of the to check the compliance of regulations.

(This story has not been edited by Business Standard staff and is auto-generated from a syndicated feed.)

First Published: Fri, August 31 2018. 21:12 IST